The following
review (of all other material following below) was received by Abco
Research
Associates on 1-21-09 from Wayne in Hawaii.
We are posting if for your information.
What Works best for me in the Long Term
This shows the finalized setup of the
Venus 2000 that has
proven most versatile and satisfactory over the very long term. It
addresses
several fiddly and major problems, mostly having to do with use of the
Venus
2000 in an actual setting.

Foremost of these are sound isolation
from the environs. The
Venus 2000 is quiet, but it does make noise. It is heavy and that
causes solid
acoustic contact with whatever it is placed on. This can result in
serious
noise by conduction through a structure. Sound isolation is as simple
as
disconnecting the unit from the building structure.
The base used for this purpose is
further pressed into
service to provide a support arm to manage the hoses and controls more
easily.
Other things to note in the above
photo include the use of
spiral wrap cable binding to merge the stroke control hose and the hand
control
wiring into a single bundle which in turn is hung from the end of the
adjustable support arm at a convenient place to take stress off the
fittings on
the Venus 2000 and also to help control these items.

This is the base plate. The vertical
arm is old salvaged
monkey bars used in laboratories for apparatus support. It is half inch
aluminum rod. The crossbar is the same stuff and the joiner, the
coupler, is a
standard accessory for joining two at right angles while allowing them
to be
adjusted in both directions with thumb screws. Note the drilled
recesses for
the four feet.

The original ABCO feet were replaced
with these taller
cylinder hard rubber feet. These fit into the depressions in the base
board and
prevent any sliding about. They are so tall they allow for good
ventilation
under the unit even when dropped 1/4 inch into the depressions.

Simple foam padding and a second
board goes into the stack
under the base plate. Sound isolation depends on dissimilar materials
as well
as vibration isolation, so including a stiff layer between two foam
layers such
as cardboard or wood really helps. Spray adhesive could be used to bind
these
together but I just leave them loose. The foam is non-skid enough to
keep
things from moving about too much.

Here is the entire stack assembled.
This completely prevents
sound from being conducted into the structure. Only air born sound,
which is
easy to suppress, is left and it is relatively minor even under heavy
load.
Note how the feet fit into the depressions and still leave plenty of
ventilation under the Venus 2000 unit.
Control Units
Merged
A major problem is the running away
of the controls for both
air and speed during use. They seem to love to exist on the floor. Two
things
were done to control this. First of all the two were merged.

A small metal plate was cut to fit
the two side by side and
drilled with a hole for a large split ring. Then a simple badge holder
was
attached with a swivel. The units were mounted in a very simple way
that has
proven very sound. Thick double sided tape was used. This stuff is like
a clear
gel about 1/8 of an inch thick and very tacky. It allowed one to deal
with the
recesses on the bottom of the units and get a very firm install that
has stayed
in place for years
With these two units merged into one,
the remaining problem
was their love for running for the floor at the first chance. I found a
simple
solution was installation of four rubber feet on the back of the new
plate
which has helped immensely. Finally the badge clip can be fastened to a
fold in
a sheet or similar fabric area to restrain it further. The support arm
can be
positioned to take the weight of some of the cord and hose to further
decrease
the love of floor this unit shows.

Here you can see the feet and the
badge clip from the
backside view of the dual mounting plate. This has been just great and
solves
the problem that the single speed controller already had and which was
multiplied when there were two such units to constantly be sliding onto
the
floor at every chance.

This was a good idea not carried far
enough. The idea was to
make the buttons different in a tactile sense to help know if your
finger was
on the in or out valves of the controller. Having the units merged into
one
helps a lot with this since now on is in the middle of the combo and
one is at
one end of the combo, no longer symmetrical. But this idea does work.
The
engraved cross cut with a simple hack saw blade just needs to be more
dramatic
and deeper.
Hose Clamp
added to Main Air Hose

One problem that I did have was the
taper on the feed hose.
It constantly expanded the hose over time and it became loose and
slipped off
easily. Cutting back the hose an inch or so solved this problem. But I
finally
just cut off a fresh 1 foot length of hose and even cut off some of the
hose
fitting itself to increase its ID. Then I used a small hose clamp to
firmly
attach the short hose to the unit. Then I used a double ended barbed
plastic
fitting which had been cut back to the correct ID range to reduce
constriction
to join to the actual hose.

I am very happy with this
modification. It has proven
worthwhile. The plastic joins come for a wide range of sizes and you
just cut
them at a barb which gives the proper ID which considerably decreases
flow
resistance when used with the larger hoses. They originally work for
sizes from
1/8th inch to 1/2 inch, so the terminal ID is very small.
Summary:
- The combining of
both controls onto a single plate which has rubber feet on the back and
a badge clip on a swivel to help control its hyper irritating fondness
for the floor has been a fantastic frustration reliever. It is highly
recommended. The use of thick 3M brand double sided adhesive "tape"
which is actually a gel with a thick red peal off backing has proven
ideal. This stuff makes a very firm mounting where space filling is
also needed.
- The use of a sound
isolation plate is wonderful. It eliminates the main source of noise
pollution, conduction through the structure. The trick is to use longer
feet and depressions drilled into the base plate. I used a simple wood
spade drill in a drill press to make the depressions, setting the drill
press stop to make them even. The base is just some laminate covered
junk pressboard I had on hand in the scrap pile. The plastic laminate
coating meant I did not have to paint it and it wipes off easily for
cleaning and dusting.
- Other bits are
minor but work well for me. The use of a hose clamp on a short adapter
hose to eliminate completely the slippage of the main receiver hose
after it flares out with time has been a long term solution. The use of
a cross bar with fancy clamp to make an adjustable support arm to help
control the weight of the wire and hose to the hand units to help
encourage them to "STAY!" is also nice. The use of spiral wrap to
bundle the hose and wire together was easy and seems to also help keep
things organized and where you put them but it does make the assembly
stiffer which can help keep things in place or hinder it. Personal
choice. Works for me.
Final Note: I find the 15:1 version
of the Venus 2000 the
ideal unit. .I would recommend it to every new user. The older 10:1
unit is OK,
but the newer speed range is stronger on the bottom end and more than
fast
enough on the top end. The gear reduction of the 15:1 is just a better
fit for
the application in my opinion.
Manufacturers Note:
The 15:1 is the only unit available and is what is shipped on all new orders.
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